So , I autoxd my car this weekend. Man was it strong. Need to dyno it still but what a huge difference. I placed 3rd overall. Not too shabby w my 235 Starspecs.
Monday, after a 600mile weekend, on a datalogging run my crank pulley decided go it's own way. The crank pulley bolt loosened up and my cam timing was gone. so here is what the car looks like now.
I have not determined yet if there was any valve to piston contact, though I dont think so as everything looks ok from the top and the motor spins freely. Also I never heard a bang, crunch or otherwise. Hoping (though that is probably too soft a word) that I will just need to put a new pulley bolt in and retime the thing.
The weird thing is that I tightened the main bolt down to spec. 100Nm and then 90deg. Not sure what happened. I talked w Cosworth to see if they had any tips and they said that they use loctite on the bolt but still tighten the bolt to factory spec as I did. Ugghh
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